View Single Post
  #8  
Old 07-14-2021, 05:35 PM
Gary H's Avatar
Gary H Gary H is offline
Ultimate Warrior
 
Join Date: Feb 2002
Location: Jacksonville
Posts: 1,333
Default

I just did a 4 speed conversion for a 70' GTO and used pedals and linkage parts from our host. After finishing, I couldn't get the clutch play adjusted right for nothing. If I got a little play with the peddle up, it was out of adjustment at the bottom, and visa versa. I finally pulled the transmission back out and found the clutch fork was the incorrect length from the clutch pushrod to the pivot point where the clutch ball sits. That's comparing it to several original clutch forks I had laying around. Also, the clutch Z-bar had a lot of slop at it's pivot points and therefore was flexing. I put stock components back in, and reinstalled the transmission AGAIN, and it was good to go.

__________________
62' Lemans, Nostalgia Super Stock, 541 CI, IA2 block, billet 4.5" crank, Ross, Wide port Edelbrocks, Gustram intake, 2 4150 style BLP carbs, 2.10 Turbo 400, 9" w/4:30 gears, 8.76 @153, 3100lbs